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Once
the metal jacket strip was tight against the block, I put the block in our
oven in the kitchen for 10 minutes at 250 degrees. (Do this while your
wife is away for the day) When I removed the block from the oven, I
started to weld on top of the block, from the intake side, to the exhaust
side of the block I used Stainless welding rod with my arc welder. I tried
welding rod made for cast iron, but the stainless proved to be the best..
When you start to weld the jacket, you welded as fast as possible before
the block lost its oven heat. If you did not preheat the block, you could,
and often did crack some of the fins. Once the main jacket was welded on
the hard part began; now you had to make small pieces to fit into the
areas not covered by the bigger jacket. It normally took the better part
of a day to prepare the pieces needed and to weld up a water jacket on a
motor. I wish I could tell you that the water cooled Cushman was the best.
It was in many ways the best for me, but there were several air cooled
Cushman engines from North Carolina and California that I was never able
to outrun. The builders of these engines were Frank Jarrell, of
Kemersville, N.C., and Frank Kiler of Visalia, Ca.
Now
that we have pretty well run through making a water cooled block, I will
mention some of the other things that help make this motor stay together
and run better. The crankshaft on a Cushman engine is way out of balance.
When I first tried to balance the crankshaft I drilled holes in the
counter weights, packed the holes with lead, and welded a steel plug to
cover the holes. A lot of work, and I never could get enough lead into the
crank to bring it into balance. I finally welded a steel plate much like
you can buy today on the counter weight. Since we never had the cranks
ground to under size, welding this in place worked the best for us. The
plate was cut from 1/4 inch steel and was a bit larger than the stock
Cushman. The rod, while being one of the strong points of the motor, had a
weakness in the area of the 4-rod bolts. The straight cut where the head
of the rod bolts were left a shear point where the rod almost always
broke. We brazed this area and filled it with brass, covering the head of
the rod bolts and then shaping it to give it a rounded appearance. This
cut down on the broken rods a great deal. I normally changed rods every
month, five each racing season, as a mater of good maintenance. The
crankshaft bearing spacing was a weak point, in that they are so far apart
and allow the crankshaft to flex near the rod journal, which leads to it
breaking at that point. I did break several crankshafts early in my racing
career, one time it destroyed the block and camshaft. I learned early in
my racing to change the crankshaft every month to 6 weeks. Here again,
just good maintenance. On one of the motors the crank broke and the
connecting rod hit and bent the camshaft. I put this camshaft in a press
to straighten it and for some reason it became one of my best. It was only
in later years that I understood that bending it and then pressing it back
straight changed the lobe centers. For some reason this cam made a motor
run like the "Bat out of you know where." Previously in this
article I gave you the degrees for the cams made by Bob Sawyer. Almost all
the cams I bought from Bob would give you between.280 to.300 valve lift.
Here again, some people would like to lift the valves to the moon, but you
can only flow so much thru a valve, and this amount of lift proved to work
well. I once took a cam blank to Iskenderian's in California to get a
change in the grind. This was not the main Ed Iskenderian shop that
everyone knows about, but his brother Luther who had a shop behind the
main building where he did motorcycle cams. He was so excited when I told
him it was a cam for a Cushman. He said he had driven a Cushman Airborne
all over the Philippines when he was in the service in WW2. When I told
him the size of the valves, and the valve spring seat pressure of 80
pounds he was honest with me and said I had a good cam for what I wanted
to do with the cam grinds made by Bob Sawyer. I did, on several occasions,
machine my own cam blanks on my lathe and had the cams ground by Effingham
Cam Grinders in Effingham, Illinois.
When I went to
the water-cooled motor, piston seizing was a thing of the past as the
motor ran so much cooler now. We replaced the piston clips with Teflon
buttons. The clips had a tendency to crystallize and break, in doing so
destroy the cylinder wall. We reamed the piston so that the wrist pin
floated back and forth, with the Teflon buttons pressed in each side
contacting the cylinder wall. Cushman did this early on with some of their
first motors, except they used aluminum plugs, or buttons as we call them.
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To
set the end gap for a ring place down it in the bore of the motor and,
with a feeler gauge, find how much gap you have. To increase the gap place
a fine file straight up in your bench vice and, with a side of the ring in
each hand, place the ring with a side on each side of the file, and hold
the ring ends tight against the file and draw the ring up and down on the
file. This way you take a equal amount off of each end of the ring. Keep
putting the ring back in the bore of the motor and checking with the
feeler gauge so that you do not open the gap too much. When you have done
this with all three rings, place them on the piston. Cushman, in all their
literature, fails to tell you where to place ring on the piston after you
gap it. Gap the rings on the side of the cylinder opposite the intake and
exhaust. The bottom ring should be set so that the gap is straight across
the piston from exhaust valve. The 2nd ring gap is across the piston from
the intake valve and set the top ring is gap across the piston in
line with
the exhaust valve. With the rotation of the motor, and rod angle, this
allows the rings to maintain the gap you have set, even close this gap a
bit on the power stroke. The spark plug we used was Champion 14 mm J
series. The J series was a marine plug that gave a number of heat ranges
to work with, Most of the time we used a J2 or J4 for a hot day, or a J6
for a normal day, or cool evening. A good spark plug with methanol fuel
was a must.
Now
that I have explained as best I could about the Water Cooled Cushman, I
hope the things we have discussed will give you a few things you can use
on building your next scooter motor. I know some of what we talked about
may sound strange to some, and some will think I don't know what I am
talking about (they still think the world is flat but these are things
that worked well for me, I am just passing them on to you.)
I
have just finished restoration of my 1960 Standard Eagle in the last 3
months. I put the motor together with lash caps on the lifters, and
Wisconsin valves and heavy valve springs. The Wisconsin valves gave me
longer valve stems to work with, which gave me a better choice of valve
springs. The cam is a stock Cushman that I ground a new profile on. When I
put a degree wheel on this motor, I got what I was trying to accomplish, a
split over lap. The intake opens 77 degrees before top dead center and
closes 35 degrees after bottom dead center. The exhaust opens at 77
degrees before bottom dead center and closes 35 degrees after top dead
center. Intake valve lift is
.282 and exhaust is .280.
Photo of Bob's Test Stand
I
am just breaking the motor in so I have not opened it up yet, but I am
sure this motor will run well. I got so tired years ago of mounting a
motor on a newly painted scooter, and then having to take it off for some
reason and damaging the paint in the process so built the motor break in
stand that you see in the picture. I have an attachment that bolts where
the gray motor block is shown for polishing aluminum racing wheels. That
is why the 3/4 electric motor is installed. I also have a 2 HP electric
motor that I bolt in place of the 3/4 HP when I break in a Cushman motor.
I can start the Cushman and leave it running on the stand, or I can remove
the spark plug wire and put it on a second plug laying alongside the motor
and allow the electric motor to turn the Cushman. Since the motor turns
1140 RPM it is just right to run the engine for an hour or two to make
sure the rod bearing fit is right, and I can also check the output of the
magneto lighting coils at that time. After an hour or two with the
electric motor I fire up the Cushman, regulate the RPM’s, and run it
until it comes up to operating temperature (or until my neighbor has had
enough). Then I may run it again the next day for the same amount of time.
When I put it on the scooter it has time on it and I know it is going to
run like I planned.
I
wish all of you the very best, and keep those Cushman Scooters running
Your
California Cushman Friend Bob Jungbluth
Bob raced the Cushman engine for many years and set many records. His
need for engine parts resulted in frequent visits to the scrap yard in
Lincoln, NE to pickup parts that the Cushman Motor Company was discarding.
The parts he salvaged helped save the Cushman Scooter. I
thank Bob very much for writing this article for the web site. -Ed
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